i hate my car *thanx 2gn members*

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unsuper man
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i hate my car *thanx 2gn members*

Post by unsuper man » Thu Jan 13, 2005 6:10 pm

if it wasnt for the fact that i got forged intenrals for xmas id junk this POS neon tonight.

newest problem: car acts like it has a boost leak. wont go into boost, dosnt blow off. BUT its acting really weird. the car dsont smoke or run too hot, but at idle and while driving it seems to have a REALLY loud idle that it never had before, and it sounds like an exhuast leak, but i cant find on anywhere. also it pops ALOT all the sudden when deceleratng even in 5th at like 1500rpms, its still pops really loudly, and it dosnt seem to be coming from the rear of the exhuast. and i checked for boost leaks and vacumm leaks and found NONE....
so i think maybe my turbo is toast, but its not smoking...so what else could be wrong...can turbos go bad and not smoke and still spin at idle ( i have no intake so i can feel the wheel spinning at idle) im lost and right now the car is pissing me off....
Last edited by unsuper man on Fri Jan 14, 2005 6:03 pm, edited 1 time in total.
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noTe
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Post by noTe » Thu Jan 13, 2005 6:21 pm

How exactly does it idle? Is it jumping in RPMs or just staying in high RPMs?
noTe / randy

2004 Dodge SRT-4 BPU
1987 Honda Accord LX-i

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ram50rocket
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Post by ram50rocket » Thu Jan 13, 2005 6:31 pm

From the little bit of conquest experience I have, I think I can narrow it down for you. Either you have a wastegate problem, possible blown head gasket, or something wrong in that area deffinitely.
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89 Ram50 engine swap???
05 SRT-4 deburred
02 ACR, R.I.P. thx 4 nothin Insurance Co.
00 ES traded in 4 ACR
titansxt wrote:I hear the whats it called, Dodge Neon, is a good car.
you could probably go get your "umadbro" polished up to make it look like a new comeback again

unsuper man
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Post by unsuper man » Thu Jan 13, 2005 6:33 pm

it just idels loud. and its not blowing smoke, so how can it be a head gasket?>
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ram50rocket
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Post by ram50rocket » Thu Jan 13, 2005 6:33 pm

Oh, and it could also be a cracked exhaust turbo manifold.
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89 Ram50 engine swap???
05 SRT-4 deburred
02 ACR, R.I.P. thx 4 nothin Insurance Co.
00 ES traded in 4 ACR
titansxt wrote:I hear the whats it called, Dodge Neon, is a good car.
you could probably go get your "umadbro" polished up to make it look like a new comeback again

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dawm
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Post by dawm » Thu Jan 13, 2005 6:33 pm

hehe, i think you pissed off the NGC
12 Subaru WRX hatch - #notadowngrade
04 Neon - #base2SRT #24NAprojectgoneSRT
03 Subaru Forester 2.5XS - #gfscar #butiown
06 Subaru WRX STi - #traded4hatchback12WRX #gone
98 Neon R/T 2.4L Turbo Coupe - #7yearproject #SRTified #megasquirt
http://www.st1ck3rs.com
http://www.detroitneonowners.org

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ram50rocket
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Post by ram50rocket » Thu Jan 13, 2005 6:38 pm

I've never experienced a turbo going bad myself. Sounds more like that's the problem. I'm not much of a help, :lol: But, if everything is louder, something's broken on the outside. You'd probably here rattling if the maniflod was cracked but not nessecarily, plus you'd probably see smoke. Head gasker blown and you should see smoke also, true. Not sure how a wastegate can go bad exactly.
Image
89 Ram50 engine swap???
05 SRT-4 deburred
02 ACR, R.I.P. thx 4 nothin Insurance Co.
00 ES traded in 4 ACR
titansxt wrote:I hear the whats it called, Dodge Neon, is a good car.
you could probably go get your "umadbro" polished up to make it look like a new comeback again

noTe
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Post by noTe » Thu Jan 13, 2005 6:42 pm

Did you buy the turbo new? What size is it? List your mods
noTe / randy

2004 Dodge SRT-4 BPU
1987 Honda Accord LX-i

unsuper man
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Post by unsuper man » Thu Jan 13, 2005 7:01 pm

teo4h, form a lebearn, it was rebuilt when bought, and it dosnt smoke and spins at idle. i have a stock srt fmic, custom ic piping, HKS ssqv, log manifold, and i donno other non turbo related things, msd dis2, wires...
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diablo25mn
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Post by diablo25mn » Thu Jan 13, 2005 7:27 pm

it you hear a loud choppy sould, most likely you have an exhuast leak either at the manifold flange or at the turbo flange. Whats your vacuum readings? Check your oil does it seem watery? Check your spark plugs what color are they? What Gap did you set them at? What gap are they now? Do you have a catch can? How much oil is inside the catch can? Lastly check your codes, anything that is not normally there?
I would post a mod list, but Its too long and i'm way too lazy....
http://www.floridaneons.org/forums/albu ... user_id=22

unsuper man
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Post by unsuper man » Thu Jan 13, 2005 8:03 pm

would fouled plugs keep me outta boost some how? vac is a normal 20. i have a weirdo map not matching TPS code, but the car ran ok when i got that code a few days ago. i have no catch can.

air hsould be coming outta the port on the back of the vlave cover right?
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diablo25mn
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Post by diablo25mn » Thu Jan 13, 2005 10:22 pm

Plugs could be the cause, my friend in his srt could make a care go from screamer to just plain ol shit that needs to be flushed, did you check the gap, make sure you didn't detonate , one sign of this is the electrode on the tip of the spark plug closing more than the initial gap you said it at (like going from .35 to .25). How's the oil? If you're not seeing any boost, check the wastegate the swing valve might be the problem.
I would post a mod list, but Its too long and i'm way too lazy....
http://www.floridaneons.org/forums/albu ... user_id=22

unsuper man
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Post by unsuper man » Thu Jan 13, 2005 10:49 pm

wg's are fine. ill check the spark plugs, the care seems to run fine other then tis not getting into boost...
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diablo25mn
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Post by diablo25mn » Thu Jan 13, 2005 11:33 pm

do you have any way of check to see what boost you read on the turbo directly. I'm beginning to if your compressor wheel is actually spinning with the turbine wheel and not just rotating on the bearings. Honestly if the wastegate isn't bad then the only other option is to pull the turbo and find out if the bearings or even the wheel shaft is still intact. :?
I would post a mod list, but Its too long and i'm way too lazy....
http://www.floridaneons.org/forums/albu ... user_id=22

unsuper man
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Post by unsuper man » Fri Jan 14, 2005 4:38 pm

i can feel the wheel spining when its at idle, as i dont run an intake, but theres nothing stuck in it and no sign of damage....
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unsuper man
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Post by unsuper man » Fri Jan 14, 2005 6:05 pm

i figured it out, but thank you to everyone who help trobule shot it, it was a combination of things, i run 2 wastegates, internal, and a external 38mm. along wiht the internal being jaammed open, the bolts ont he external were lose, and i did have a hole in a coupling from where my ic hits parking curbs, it seems to be running ok now, but ill keep you posted.
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Nino@MODTECH
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Post by Nino@MODTECH » Fri Jan 21, 2005 3:08 am

What are you using for fuel control? Rising rate fuel pressure?
MODTECH AUTOSPORTS

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