Post
by LCPLPunk » Mon Dec 12, 2005 10:42 pm
gonna keep it just like it is.
I had a big scare today guys...
Iwent with my installguy and we drove around and tried to tune it, but it seemed when i floored it that it wasn't any faster than stock. My guy said it was my ATX tranny, but i knew something was wrong.
To make matters worse the wideband scraped on the floor and stopped working, so forget finishing the tuning. Anyways, i get home and talk to EvilCreations and Evo Neon and they say i've got a boost leak, so..i check all my hoses, and in the process i find that one of the hoses completely came out of it's silicon coupler, so hte air was basically blowing out. I found out the pipe was too short, so i had to run to Midas to get one, and with the new pipe..we have.......BOOOOOOOST!
Only 4psi or so, but on Wednesday i'm gonna go get it tuned on the dyno at 8psi, and we'll see how it works then.

The good news is, i fabbed
2001 Neon R/T
Deyeme Motor Mounts, Booger Bushings, JohnnyMopar Cradle Bushings, SRT Silver shift knob, Maddog STS, SRT Rear Seat, K&N WAI, Magnecore Wires, Mobil 1 Full Synthetic Oil, Coil pack heat shield
""The bitterest tears shed over graves are for words left unsaid and deeds left undone" - Harriet Beecher Stowe"